Blowout During a Completion Operation with a Snubbing Unit
Wild Well Control (WWC) Personnel responded to a blowout on a completion operation on a multi-well pad in Ohio. This project was completed by removing the rig, snubbing unit, and capping the well. The client was then able to return to normal operations.
This incident occurred while drilling out plugs in a post-fracture stage of the completion. The cause was suspected to be movement of the wellhead, BOP, and snubbing unit while drilling out the plugs. This instability at the wellhead was noted upon arrival and is suspected to be the primary reason for the wellhead component failure. During the drilling operations, the wellhead and snubbing equipment was reported to have demonstrated slight freedom of movement. The tubing spool wing valve was tied into a flow line to the gas production equipment on location. This line was buried and did not move along with the
wellhead components, placing stress on the connection at the wellhead. The flanged connection at the tubing spool wing valve and the wellhead ultimately failed and begin to leak. The leak quickly intensified, and the location was evacuated.
WWC personnel were successful in the removal of the workover rig, snubbing unit, and the tubing spool. The well was capped and shut-in with a single-blind ram to contain the wellbore. The client then proceeded with the final workover to install a new tubing spool and continue with the well operations.
Most well control operations involve multiple phases to achieve the ultimate goal of regaining control of the well. The following operational phases were completed for this project to reach the final resolution.
In some cases, it may be possible to kill the well to allow intervention operations to proceed. In this case, the snubbing work string was in the lateral section of the wellbore drilling plugs when the event occurred. This provided the necessary conduit to attempt a kill attempt. The kill attempt was made with a 16.5 ppg OBM. Mud returns were noted at the exit early on, suggesting that the tubing had been subsequently compromised. The kill attempt was abandoned, and the operations progressed to the next phase.
The plan then moved toward the removal of the failed tubing spool. This would require the removal of the workover rig, snubbing unit, BOP equipment, and frac valves. Along with direct actions to the subject well, the adjacent wells had protective cages installed to limit possible escalation. These were fabricated by the client and installed over the 3 additional wells on the pad.
The tubing was cut in the snubbing basket to allow the power swivel to be removed. The rig blocks were secured to the derrick and the tubing board was removed with a crane. The workover rig hydraulic system was plumbed into an auxiliary source and the derrick was scoped in and laid down, allowing the rig to be removed from the well site. With the rig removed, operations proceeded to the next phase.
The next phase of the intervention was to make an abrasive jet cut on the lower frac valve. The snubbing unit, BOP equipment, and frac valves would all be removed with the crane upon completion of the cut. The crane was tied onto the snubbing unit lifting bridle and the necessary pumping equipment was rigged up and tested for the abrasive cut. The WWC Abrasive Jet Cutter (AJC) was installed on an Athey wagon and the cut was completed without issue. The snubbing unit and additional components on the stack were removed leaving the tubing spool and bottom flange from the lower frac valve. The crane was tied to the tubing spool and the spool was removed from the casing spool – thus removing the failed component from the wellhead. The capping BOP could now be installed on the casing spool for securing the well.
The capping stack for this operation was a single-blind ram. The well was planned to be shut-in and would not require any diversion as the previously failed tubing spool was now removed, and the original wellhead that was installed was unaffected by the event. The capping BOP was landed on the casing spool with no issues and closed, securing the flow from the well. The client began planning the wellbore recovery operations.